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<article xml:lang="EN" xmlns:mml="http://www.w3.org/1998/Math/MathML" xmlns:xlink="http://www.w3.org/1999/xlink" article-type="case-report">
<front>
<journal-meta>
<journal-id journal-id-type="publisher-id">Bohr. Amr.</journal-id>
<journal-title>BOHR International Journal of Advances in Management Research</journal-title>
<abbrev-journal-title abbrev-type="pubmed">Bohr. Amr.</abbrev-journal-title>
<issn pub-type="epub">2583-6943</issn>
<publisher>
<publisher-name>BOHR</publisher-name>
</publisher>
</journal-meta>
<article-meta>
<article-id pub-id-type="doi">10.54646/bijamr.2025.40</article-id>
<article-categories>
<subj-group subj-group-type="heading">
<subject>Case study</subject>
</subj-group>
</article-categories>
<title-group>
<article-title>Applying Six Sigma and design of experiment to improve coil manufacturing processes &#x2013; a case study in KSVN</article-title>
</title-group>
<contrib-group>
<contrib contrib-type="author" corresp="yes">
<name><surname>Nhu</surname> <given-names>Phong Nguyen</given-names></name>
<xref ref-type="aff" rid="aff1"><sup>1</sup></xref>
<xref ref-type="corresp" rid="c001"><sup>&#x002A;</sup></xref>
<xref ref-type="author-notes" rid="fn002"><sup>&#x2020;</sup></xref>
</contrib>
<contrib contrib-type="author">
<name><surname>Phi</surname> <given-names>Van Hai Dang</given-names></name>
<xref ref-type="aff" rid="aff1"><sup>1</sup></xref>
</contrib>
<contrib contrib-type="author">
<name><surname>Thi</surname> <given-names>Kim Thu Ta</given-names></name>
<xref ref-type="aff" rid="aff1"><sup>1</sup></xref>
</contrib>
<contrib contrib-type="author">
<name><surname>Nhu</surname> <given-names>Tu Anh Nguyen</given-names></name>
<xref ref-type="aff" rid="aff2"><sup>2</sup></xref>
</contrib>
</contrib-group>
<aff id="aff1"><sup>1</sup><institution>Industrial Systems Engineering, HCMC University of Technology &#x2013; VNU-HCM</institution>, <addr-line>Ho Chi Minh City</addr-line>, <country>Vietnam</country></aff>
<aff id="aff2"><sup>2</sup><institution>Faculty of Information Technology, Monash University</institution>, <addr-line>Melbourne, VIC</addr-line>, <country>Australia</country></aff>
<author-notes>
<corresp id="c001">&#x002A;Correspondence: Phong Nguyen Nhu, <email>nnphong@hcmut.edu.vn</email></corresp>
<fn fn-type="other" id="fn002"><p><bold><sup>&#x2020;</sup>ORCID:</bold> Phong Nguyen Nhu <ext-link ext-link-type="uri" xlink:href="https://orcid.org/0009-0007-9147-9318">0009-0007-9147-9318</ext-link></p></fn>
</author-notes>
<pub-date pub-type="epub">
<day>24</day>
<month>09</month>
<year>2025</year>
</pub-date>
<volume>4</volume>
<issue>1</issue>
<fpage>42</fpage>
<lpage>49</lpage>
<history>
<date date-type="received">
<day>12</day>
<month>03</month>
<year>2025</year>
</date>
<date date-type="accepted">
<day>01</day>
<month>04</month>
<year>2025</year>
</date>
</history>
<permissions>
<copyright-statement>Copyright &#x00A9; 2025 Nhu, Phi, Thi and Nhu.</copyright-statement>
<copyright-year>2025</copyright-year>
<copyright-holder>Nhu, Phi, Thi and Nhu</copyright-holder>
<license xlink:href="https://creativecommons.org/licenses/by/4.0/"><p>&#x00A9; The Author(s). 2024 Open Access This article is distributed under the terms of the Creative Commons Attribution 4.0 International License (https://creativecommons.org/licenses/by/4.0/), which permits unrestricted use, distribution, and reproduction in any medium, provided you give appropriate credit to the original author(s) and the source, provide a link to the Creative Commons license, and indicate if changes were made.</p></license>
</permissions>
<abstract>
<p>The company under study specializes in manufacturing parts for the automotive industry. The manufacturing process of the company has the problem of high failure rates (FRs), resulting in high-quality failure costs and low profit. In this research, Six Sigma was used to solve the problem with the objective to reduce the FR. The research methodology was based on the define measure analyze improve control (DMAIC) procedure, including five steps: define, measure, analyze, improve, and control. The tools used in the steps of the DMAIC procedure include cause and effect diagrams, Pareto diagrams, and control charts. In addition, design of experiments (DOEs) was also used to optimize the process parameters. After applying Six Sigma and DOE, the FR of the coil manufacturing process reduced by nearly 50%, from 10.27 to 5.33%.</p>
</abstract>
<kwd-group>
<kwd>Six Sigma</kwd>
<kwd>DMAIC</kwd>
<kwd>DOE</kwd>
<kwd>ANOVA</kwd>
<kwd>SIPOC</kwd>
<kwd>project charter</kwd>
<kwd>Pareto charts</kwd>
<kwd>control charts</kwd>
</kwd-group>
<counts>
<fig-count count="13"/>
<table-count count="10"/>
<equation-count count="2"/>
<ref-count count="8"/>
<page-count count="8"/>
<word-count count="4114"/>
</counts>
</article-meta>
</front>
<body>
<sec id="S1" sec-type="intro">
<title>Introduction</title>
<p>Nowadays, businesses all over the world are facing the challenge of quality. With globalization, competition and demand are increasing. Quality is no longer a purely technical issue but has become a top strategic issue related to the survival of businesses.</p>
<p>Kyoshin Vietnam (KSVN) is a company specializing in manufacturing components for the automotive industry, with many different types of products. Currently, the company is also striving to build a zero defect production system according to a quality management system that meets international standards.</p>
<p>Although the company&#x2019;s quality control process is implemented quite strictly, the implementation in some departments is still not effective. In addition, due to many different factors, the quality of some of the company&#x2019;s products has not yet reached the set target, the failure rates (FRs) in the process are still high, and there are still unconformable products being moved to the next process and even to customers.</p>
<p>Mold Coil Sub Assy (C23 H5) is a new product line, requiring high precision, very strict technical requirements, and very strict quality standards. Although it has gone through the trial production stage, the product quality is still unstable; there are still many scraps in the assembly and external plastic injection stages.</p>
<p>The current FR of this product is 10.27%. This is a very high rate and is unacceptable compared to the company&#x2019;s quality system. The company currently has to produce more than the order to compensate for the defect, so the product cost is high and causes a lot of waste. The company wants to reduce the FR to below 6%.</p>
<p>Six Sigma is a popular method widely used in quality improvement. In this article, the application of Six Sigma is discussed to improve the production process of KSVN, identify and eliminate the causes of failure, and minimize waste for the above product line, with the goal of reducing the FR to below 6%.</p>
</sec>
<sec id="S2">
<title>Literature review &#x0026; research methodology</title>
<sec id="S2.SS1">
<title>Literature review</title>
<p>In the mid-1980s, Motorola pioneered the use of the Six Sigma concept in measuring product quality. In the mid-1990s, General Electric was considered a model company in implementing Six Sigma projects, and the company&#x2019;s CEO, Jack Welch, used Six Sigma as the company&#x2019;s popular quality improvement solution. Later, the quality improvement solution based on Six Sigma was applied in many companies, from manufacturing to services such as Texas Instrument, Boeing, IBM, Xerox, Citibank, Raytheon, etc.</p>
<p>Six Sigma evolved from a simple capability measure into an improvement methodology aimed at achieving unprecedented levels of quality by focusing on critical characteristics and identifying and eliminating the causes of defects. Six Sigma aims for a FR of a few parts per million by effectively applying statistical principles and tools for diagnosis, problem solving, and system improvement (<xref ref-type="bibr" rid="B1">1</xref>).</p>
<p>Soar and Balanescu (<xref ref-type="bibr" rid="B2">2</xref>) introduced the history of Six Sigma as well as highlighted the benefits of applying Six Sigma. In addition, the define measure analyze improve control (DMAIC), design for six sigma (DFSS), define measure analyze design verify (DMADV), identify design optimize validate (IDOV), and difference-in-differences (DIDES) methods were introduced depending on the purpose of use. In which, the DMAIC process&#x2014;Define, Measure, Analyze, Improve, and Control&#x2014;was described specifically, and they also introduced how to apply Six Sigma in process management.</p>
<p>Gupta (<xref ref-type="bibr" rid="B3">3</xref>) presented a quality improvement study applied at a yarn manufacturing company based on Six Sigma methodologies. He applied the DMAIC process to identify, the cause of the problem and improve quality, reducing the percentage of defective yarn products.</p>
<p>Sokovi&#x0107; (<xref ref-type="bibr" rid="B4">4</xref>) presented a Six Sigma project, undertaken within the company for the production automotive parts, which deals with the identification and reduction of production cost in the deburring process for gravity die-castings and the improvement of the quality level of produced parts.</p>
<p>Ferreira and Lopes (<xref ref-type="bibr" rid="B5">5</xref>) used Six Sigma methodology in a semiconductor company to simplify the scrap request process of electronic controllers of wall-hung gas boilers and to reduce its processing time. Through the elimination of problems identified and resolved using the DMAIC procedure, the processing time of scrap requests was substantially reduced, allowing for high cost savings.</p>
<p>Hung and Sung (<xref ref-type="bibr" rid="B6">6</xref>) used Six Sigma to solve an underlying problem of reducing process variation and the associated high FR in a food company in Taiwan. The DMAIC phases were utilized to decrease the FR of small custard buns by 70% from the baseline of 0.45% to below 0.141%.</p>
<p>Kurnia et al. (<xref ref-type="bibr" rid="B7">7</xref>) determined the level of sigma defects of socks and provided suggestions for quality improvements in reducing the percentage of sock defects. The methodology used in the study is the DMAIC approach. The results of this study are that the level of Sigma increased from 3.7017 to 3.9614, and the percentage of sock defects decreased from 11.08 to 5.54%.</p>
<p>Nguyen Nhu et al. (<xref ref-type="bibr" rid="B8">8</xref>) applied Lean Six Sigma to improve garment production processes. The research methodology was based on Lean Six Sigma theory, with the platform of the DMAIC procedure. The tools used in the steps of the DMAIC procedure include cause-and-effect-diagram, Pareto diagram, value stream management, work design, single-minute exchange of dies (SMED), line balancing, Kanban systems, first in first out (FIFO), autonomous maintenance, visual management, design of experiments (DOEs), and control charts. After applying Lean Six Sigma tools, the company had reduced the production lead time by 89.21% from 279 to 30.1 min, reduced the production cycle time by 36% from 25 to 16 s, and reduced the process defect rate by 37.45% from 14.9 to 9.32%.</p>
</sec>
<sec id="S2.SS2">
<title>Research methodology</title>
<p>Six Sigma is a rigorous, data-driven improvement approach with specific problem-solving steps. Six Sigma uses sophisticated statistical tools with a tightly structured problem-solving approach based on the scientific research methodology, including five steps:</p>
<list list-type="simple">
<list-item>
<label>1.</label>
<p>D &#x2013; Define</p>
</list-item>
<list-item>
<label>2.</label>
<p>M &#x2013; Measure</p>
</list-item>
<list-item>
<label>3.</label>
<p>A &#x2013; Analyze</p>
</list-item>
<list-item>
<label>4.</label>
<p>I &#x2013; Improve</p>
</list-item>
<list-item>
<label>5.</label>
<p>C &#x2013; Control</p>
</list-item>
</list>
<p>The define step identifies the problem, the objective, the product line to be improved, and the scope of the manufacturing process. Tools used in the define step include Pareto charts, suppliers inputs process outputs customers (SIPOC), and project charter.</p>
<p>The measure step collects data to measure the actual capacity of the process through the capacity of the stations. The tool in the measure step is a check sheet to collect data.</p>
<p>The analysis step finds the root causes of the problem, from which solutions are proposed to solve the problem, including the following sub-steps:</p>
<list list-type="simple">
<list-item>
<label>1.</label>
<p>Identify critical stations with high FRs.</p>
</list-item>
<list-item>
<label>2.</label>
<p>Identify root causes in the critical stations.</p>
</list-item>
<list-item>
<label>3.</label>
<p>Identify solutions for the root causes.</p>
</list-item>
</list>
<p>Tools used in the analysis step include cause effect diagram (CED), Pareto charts, and 5 Whys.</p>
<p>The improvement step implements the solutions identified in the analysis step to improve the process to achieve the goals set in the define step. DOEs is used in this step to optimize the process parameters.</p>
<p>The control step controls the process to maintain improved results. Control charts are tools used to control critical quality characteristics of the process.</p>
<p>The DMAIC procedure would be used to improve the production process of KSVN as presented in the following sections.</p>
</sec>
</sec>
<sec id="S3">
<title>Define</title>
<p>Low quality reduced external customer satisfaction and caused great waste for the company. The company had nine product families, including C23, B71, B60, 7PC, V13, CB7, G50, and A01. For product line selection, the Pareto chart of revenue R and cumulative revenue percentage CRP of product families was shown in <xref ref-type="fig" rid="F1">Figure 1</xref>.</p>
<fig id="F1" position="float">
<label>FIGURE 1</label>
<caption><p>Pareto chart of revenues.</p></caption>
<graphic mimetype="image" mime-subtype="tiff" xlink:href="bijamr-2025-40-g001.tif"/>
</fig>
<p>The Pareto chart of FR and cumulative failure rate (CFR) product families was shown in <xref ref-type="fig" rid="F2">Figure 2</xref>.</p>
<fig id="F2" position="float">
<label>FIGURE 2</label>
<caption><p>Pareto chart of FRs.</p></caption>
<graphic mimetype="image" mime-subtype="tiff" xlink:href="bijamr-2025-40-g002.tif"/>
</fig>
<p>From the two Pareto charts in <xref ref-type="fig" rid="F1">Figures 1</xref> and <xref ref-type="fig" rid="F2">2</xref> above, it could be seen that product family C23 has both the highest revenue and the highest FR. Therefore, product family C23 is selected for further analysis. Product family C23 included many products with CFRs as shown in <xref ref-type="table" rid="T1">Table 1</xref> below.</p>
<table-wrap position="float" id="T1">
<label>TABLE 1</label>
<caption><p>CFRs of products in the C23 family.</p></caption>
<table cellspacing="5" cellpadding="5" frame="hsides" rules="groups">
<thead>
<tr>
<td valign="top" align="left">i</td>
<td valign="top" align="center">Products</td>
<td valign="top" align="center">FRs (%)</td>
<td valign="top" align="center">CFRs (%)</td>
</tr>
</thead>
<tbody>
<tr>
<td valign="top" align="left">1</td>
<td valign="top" align="center">C23 H5</td>
<td valign="top" align="center">10.27</td>
<td valign="top" align="center">59.65</td>
</tr>
<tr>
<td valign="top" align="left">2</td>
<td valign="top" align="center">C23 H6</td>
<td valign="top" align="center">2.64</td>
<td valign="top" align="center">74.96</td>
</tr>
<tr>
<td valign="top" align="left">3</td>
<td valign="top" align="center">C23 H7</td>
<td valign="top" align="center">2.28</td>
<td valign="top" align="center">88.20</td>
</tr>
<tr>
<td valign="top" align="left">4</td>
<td valign="top" align="center">C23 H8</td>
<td valign="top" align="center">2.03</td>
<td valign="top" align="center">100.00</td>
</tr>
</tbody>
</table></table-wrap>
<p>From <xref ref-type="table" rid="T1">Table 1</xref>, C23 H5 was the product with the highest FR. This was also a new product with unstable quality compared to the remaining products in the C23 family. This product was required to satisfy strict technical requirements from customers. Therefore, this product was selected for further research. C23H510 0020 included parts and semi-products as described in <xref ref-type="fig" rid="F3">Figure 3</xref>.</p>
<fig id="F3" position="float">
<label>FIGURE 3</label>
<caption><p>Parts in C23 H5.</p></caption>
<graphic mimetype="image" mime-subtype="tiff" xlink:href="bijamr-2025-40-g003.tif"/>
</fig>
<p>In order to get an overview and the scope of the manufacturing process of the selected product before starting the steps of measuring, analyzing, and improving the process, the SIPOC diagram is used as shown in <xref ref-type="fig" rid="F4">Figure 4</xref> below.</p>
<fig id="F4" position="float">
<label>FIGURE 4</label>
<caption><p>The suppliers inputs process outputs customers (SIPOC) diagram of the selected product.</p></caption>
<graphic mimetype="image" mime-subtype="tiff" xlink:href="bijamr-2025-40-g004.tif"/>
</fig>
<p>KK was the supplier and also the customer. Inputs include materials such as copper wire, plastic beads, etc., from suppliers, and machinery such as welding machines, wire winding machines, plastic injection machines, testing machines, and packaging machines. The process included 9 stations as in <xref ref-type="table" rid="T2">Table 2</xref>. The output was C23 H5.</p>
<table-wrap position="float" id="T2">
<label>TABLE 2</label>
<caption><p>Work stations in the process.</p></caption>
<table cellspacing="5" cellpadding="5" frame="hsides" rules="groups">
<thead>
<tr>
<td valign="top" align="left">Work stations</td>
<td valign="top" align="left">Functions</td>
</tr>
</thead>
<tbody>
<tr>
<td valign="top" align="left">W1</td>
<td valign="top" align="left">Bobin plastic injection</td>
</tr>
<tr>
<td valign="top" align="left">W2</td>
<td valign="top" align="left">Core stamping</td>
</tr>
<tr>
<td valign="top" align="left">W3</td>
<td valign="top" align="left">Terminal stamping</td>
</tr>
<tr>
<td valign="top" align="left">W4</td>
<td valign="top" align="left">Core assembly</td>
</tr>
<tr>
<td valign="top" align="left">W5</td>
<td valign="top" align="left">Terminal assembly</td>
</tr>
<tr>
<td valign="top" align="left">W6</td>
<td valign="top" align="left">Wire winding</td>
</tr>
<tr>
<td valign="top" align="left">W7</td>
<td valign="top" align="left">Soldering</td>
</tr>
<tr>
<td valign="top" align="left">W8</td>
<td valign="top" align="left">Excess copper wire processing</td>
</tr>
<tr>
<td valign="top" align="left">W9</td>
<td valign="top" align="left">Inspection of internal diameter &#x0026; appearance</td>
</tr>
<tr>
<td valign="top" align="left">W10</td>
<td valign="top" align="left">External plastic injection</td>
</tr>
<tr>
<td valign="top" align="left">W11</td>
<td valign="top" align="left">Wavelength, resistance inspection &#x0026; packaging</td>
</tr>
</tbody>
</table></table-wrap>
<p>From the information defined above, the article briefly describes as in the project charter with voice of customer, critical to quality, objective, and scope in <xref ref-type="fig" rid="F5">Figure 5</xref> below.</p>
<fig id="F5" position="float">
<label>FIGURE 5</label>
<caption><p>The Six Sigma project charter.</p></caption>
<graphic mimetype="image" mime-subtype="tiff" xlink:href="bijamr-2025-40-g005.tif"/>
</fig>
</sec>
<sec id="S4">
<title>Measure</title>
<p>In order to measure the process capability, the FR of the stations in the process was collected as shown in the following <xref ref-type="table" rid="T3">Table 3</xref>.</p>
<table-wrap position="float" id="T3">
<label>TABLE 3</label>
<caption><p>The FRs of the stations in the process.</p></caption>
<table cellspacing="5" cellpadding="5" frame="hsides" rules="groups">
<thead>
<tr>
<td valign="top" align="left">Work stations</td>
<td valign="top" align="left">Functions</td>
<td valign="top" align="center">FR (%)</td>
</tr>
</thead>
<tbody>
<tr>
<td valign="top" align="left">W1</td>
<td valign="top" align="left">Bobin plastic injection</td>
<td valign="top" align="center">0.03</td>
</tr>
<tr>
<td valign="top" align="left">W2</td>
<td valign="top" align="left">Core stamping</td>
<td valign="top" align="center">0.06</td>
</tr>
<tr>
<td valign="top" align="left">W3</td>
<td valign="top" align="left">Terminal stamping</td>
<td valign="top" align="center">0.04</td>
</tr>
<tr>
<td valign="top" align="left">W4</td>
<td valign="top" align="left">Core assembly</td>
<td valign="top" align="center">0.06</td>
</tr>
<tr>
<td valign="top" align="left">W5</td>
<td valign="top" align="left">Terminal assembly</td>
<td valign="top" align="center">0.06</td>
</tr>
<tr>
<td valign="top" align="left">W6</td>
<td valign="top" align="left">Wire winding</td>
<td valign="top" align="center">3.86</td>
</tr>
<tr>
<td valign="top" align="left">W7</td>
<td valign="top" align="left">Soldering</td>
<td valign="top" align="center">0.64</td>
</tr>
<tr>
<td valign="top" align="left">W8</td>
<td valign="top" align="left">Excess copper wire processing</td>
<td valign="top" align="center">0.10</td>
</tr>
<tr>
<td valign="top" align="left">W9</td>
<td valign="top" align="left">Inspection of internal diameter &#x0026; appearance</td>
<td valign="top" align="center">0.15</td>
</tr>
<tr>
<td valign="top" align="left">W10</td>
<td valign="top" align="left">External plastic injection</td>
<td valign="top" align="center">5.21</td>
</tr>
<tr>
<td valign="top" align="left">W11</td>
<td valign="top" align="left">Wavelength, resistance inspection &#x0026; packaging</td>
<td valign="top" align="center">0.08</td>
</tr>
<tr>
<td/>
<td valign="top" align="left">TOTAL</td>
<td valign="top" align="center">10.27</td>
</tr>
</tbody>
</table></table-wrap>
<p>It was found that the process FR was 10.27%, which is quite high. After measuring the current situation, the goal was set to reduce the product FR to below 6%.</p>
</sec>
<sec id="S5">
<title>Analysis</title>
<p>The FRs were arranged in descending order as shown in the following <xref ref-type="table" rid="T4">Table 4</xref>.</p>
<table-wrap position="float" id="T4">
<label>TABLE 4</label>
<caption><p>The FRs arranged in descending order.</p></caption>
<table cellspacing="5" cellpadding="5" frame="hsides" rules="groups">
<thead>
<tr>
<td valign="top" align="left">i</td>
<td valign="top" align="left">Work stations</td>
<td valign="top" align="center">FR (%)</td>
</tr>
</thead>
<tbody>
<tr>
<td valign="top" align="left">1</td>
<td valign="top" align="left">External plastic injection</td>
<td valign="top" align="center">5.21</td>
</tr>
<tr>
<td valign="top" align="left">2</td>
<td valign="top" align="left">Wire winding</td>
<td valign="top" align="center">3.86</td>
</tr>
<tr>
<td valign="top" align="left">3</td>
<td valign="top" align="left">Soldering</td>
<td valign="top" align="center">0.64</td>
</tr>
<tr>
<td valign="top" align="left">4</td>
<td valign="top" align="left">Inspection of internal diameter &#x0026; appearance</td>
<td valign="top" align="center">0.15</td>
</tr>
<tr>
<td valign="top" align="left">5</td>
<td valign="top" align="left">Excess copper wire processing</td>
<td valign="top" align="center">0.10</td>
</tr>
<tr>
<td valign="top" align="left">6</td>
<td valign="top" align="left">Terminal stamping</td>
<td valign="top" align="center">0.04</td>
</tr>
<tr>
<td valign="top" align="left">7</td>
<td valign="top" align="left">Inspection &#x0026; packaging</td>
<td valign="top" align="center">0.08</td>
</tr>
<tr>
<td valign="top" align="left">8</td>
<td valign="top" align="left">Core stamping</td>
<td valign="top" align="center">0.06</td>
</tr>
<tr>
<td valign="top" align="left">9</td>
<td valign="top" align="left">Terminal assembly</td>
<td valign="top" align="center">0.06</td>
</tr>
<tr>
<td valign="top" align="left">10</td>
<td valign="top" align="left">Core stamping</td>
<td valign="top" align="center">0.06</td>
</tr>
<tr>
<td valign="top" align="left">11</td>
<td valign="top" align="left">Bobin plastic injection</td>
<td valign="top" align="center">0.03</td>
</tr>
</tbody>
</table></table-wrap>
<p>In order to effectively reduce the FR, stations with high FRs will be analyzed. With the goal of reducing the FR to below 6%, stations of external plastic injection and wire winding would be selected for further analysis.</p>
<sec id="S5.SS1">
<title>The external plastic injection station</title>
<p>The types of failure at the external plastic injection station, along with the FR and CFR, were collected and statistically recorded as in <xref ref-type="table" rid="T5">Table 5</xref>.</p>
<table-wrap position="float" id="T5">
<label>TABLE 5</label>
<caption><p>Failures in the external plastic injection station.</p></caption>
<table cellspacing="5" cellpadding="5" frame="hsides" rules="groups">
<thead>
<tr>
<td valign="top" align="left">Fi</td>
<td valign="top" align="left">Failures</td>
<td valign="top" align="center">FR (%)</td>
<td valign="top" align="center">CFR (%)</td>
</tr>
</thead>
<tbody>
<tr>
<td valign="top" align="left">F1</td>
<td valign="top" align="left">Copper protrusion</td>
<td valign="top" align="center">61.19</td>
<td valign="top" align="center">61.19</td>
</tr>
<tr>
<td valign="top" align="left">F2</td>
<td valign="top" align="left">Mixed materials</td>
<td valign="top" align="center">16.99</td>
<td valign="top" align="center">78.18</td>
</tr>
<tr>
<td valign="top" align="left">F3</td>
<td valign="top" align="left">Plastic scratches</td>
<td valign="top" align="center">10.21</td>
<td valign="top" align="center">88.40</td>
</tr>
<tr>
<td valign="top" align="left">F4</td>
<td valign="top" align="left">Plastic burrs</td>
<td valign="top" align="center">2.15</td>
<td valign="top" align="center">90.55</td>
</tr>
<tr>
<td valign="top" align="left">F5</td>
<td valign="top" align="left">Terminal staggered</td>
<td valign="top" align="center">1.85</td>
<td valign="top" align="center">92.40</td>
</tr>
<tr>
<td valign="top" align="left">F6</td>
<td valign="top" align="left">Product dropped</td>
<td valign="top" align="center">1.69</td>
<td valign="top" align="center">94.08</td>
</tr>
<tr>
<td valign="top" align="left">F7</td>
<td valign="top" align="left">Scratch surface</td>
<td valign="top" align="center">1.49</td>
<td valign="top" align="center">95.57</td>
</tr>
<tr>
<td valign="top" align="left">F8</td>
<td valign="top" align="left">Broken wire</td>
<td valign="top" align="center">1.38</td>
<td valign="top" align="center">96.95</td>
</tr>
<tr>
<td valign="top" align="left">F9</td>
<td valign="top" align="left">Lack of plastic</td>
<td valign="top" align="center">1.23</td>
<td valign="top" align="center">98.18</td>
</tr>
<tr>
<td valign="top" align="left">F10</td>
<td valign="top" align="left">Oil stains</td>
<td valign="top" align="center">1.06</td>
<td valign="top" align="center">99.24</td>
</tr>
<tr>
<td valign="top" align="left">F11</td>
<td valign="top" align="left">Others</td>
<td valign="top" align="center">0.76</td>
<td valign="top" align="center">100</td>
</tr>
</tbody>
</table></table-wrap>
<p>The Pareto chart was constructed from the data in <xref ref-type="table" rid="T5">Table 5</xref> as in <xref ref-type="fig" rid="F6">Figure 6</xref>.</p>
<fig id="F6" position="float">
<label>FIGURE 6</label>
<caption><p>Pareto chart for failures in the external plastic injection station.</p></caption>
<graphic mimetype="image" mime-subtype="tiff" xlink:href="bijamr-2025-40-g006.tif"/>
</fig>
<p>The CFR of three types of failures, including copper protrusion, mixed materials, and plastic scratches, accounted for 88.4%. These three types of failures were selected for further analysis to find the root cause to eliminate these types of failures.</p>
<sec id="S5.SS1.SSS1">
<title>Copper protrusion</title>
<p>Copper protrusion occurred when the outer plastic thickness covering the coil was not sufficient or the amount of plastic injected was insufficient or uneven. Using the brainstorming method combined with consultation with experts in the production department, the possible causes of this type of failure were presented in a fishbone diagram. Data collection and analysis showed that the two main causes, accounting for nearly 80% of copper protrusion, were as follows:</p>
<list list-type="simple">
<list-item>
<label>&#x2013;</label>
<p>Inadequate injection plastic amount</p>
</list-item>
<list-item>
<label>&#x2013;</label>
<p>Improper raw material drying time.</p>
</list-item>
</list>
<p>The 5 whys method was used to determine the root causes of the two main causes. Ultimately, the root causes of the problem were as follows:</p>
<list list-type="simple">
<list-item>
<label>&#x2013;</label>
<p>High mold temperature during production</p>
</list-item>
<list-item>
<label>&#x2013;</label>
<p>No drying time was recorded on the drying drum.</p>
</list-item>
</list>
</sec>
<sec id="S5.SS1.SSS2">
<title>Mixed materials</title>
<p>Using the brainstorming method combined with consultation with experts in the production department, the possible causes of mixed materials failure were presented in a fishbone diagram.</p>
<p>Data collection and analysis showed that the two main causes, accounting for 62.96% of mixed materials, were as follows:</p>
<list list-type="simple">
<list-item>
<label>&#x2013;</label>
<p>Poor mold cleaning</p>
</list-item>
<list-item>
<label>&#x2013;</label>
<p>Inappropriate tools used</p>
</list-item>
</list>
<p>Continue to analyze these two main causes to find the root causes. The root causes were as follows:</p>
<list list-type="simple">
<list-item>
<label>&#x2013;</label>
<p>Improper gloves</p>
</list-item>
<list-item>
<label>&#x2013;</label>
<p>No mold cleaning equipment.</p>
</list-item>
</list>
</sec>
<sec id="S5.SS1.SSS3">
<title>Plastic scratches</title>
<p>Using the brainstorming method and consulting experts in the production department, the failure of plastic scratches created when taking out the product, the worker collided the product with the mold wall and dropped the product, colliding with hard objects around. The root cause is due to the worker&#x2019;s incorrect operation.</p>
</sec>
</sec>
</sec>
<sec id="S6">
<title>Wire winding station</title>
<p>The possible causes for failures in the wire winding station included broken wire, scratched wire, improper winding, and some other causes. Among these causes, improper winding was the main cause, causing 90% of the failures in the wire winding station. Further analysis shows that the root causes were due to improper winding tension and the number of turns.</p>
<p><xref ref-type="table" rid="T6">Table 6</xref> summarized all root causes after the analysis step. These root causes would be addressed in the improvement step below.</p>
<table-wrap position="float" id="T6">
<label>TABLE 6</label>
<caption><p>The root causes after analysis.</p></caption>
<table cellspacing="5" cellpadding="5" frame="hsides" rules="groups">
<thead>
<tr>
<td valign="top" align="left">Stations</td>
<td valign="top" align="left">Failures</td>
<td valign="top" align="left">Main causes</td>
<td valign="top" align="left">Root causes</td>
</tr>
</thead>
<tbody>
<tr>
<td valign="top" align="left">External plastic injection</td>
<td valign="top" align="left">Copper protrusion</td>
<td valign="top" align="left">Inadequate injection plastic amount</td>
<td valign="top" align="left">High mold temperature during production</td>
</tr>
<tr>
<td valign="top" align="left"/><td valign="top" align="left"/><td valign="top" align="left">Improper raw material drying time</td>
<td valign="top" align="left">No drying time recorded on the drying drum</td>
</tr>
<tr>
<td valign="top" align="left"/><td valign="top" align="left">Mixed materials</td>
<td valign="top" align="left">Inappropriate tools used</td>
<td valign="top" align="left">Inappropriate gloves</td>
</tr>
<tr>
<td valign="top" align="left"/><td valign="top" align="left"/><td valign="top" align="left">Poor mold cleaning</td>
<td valign="top" align="left">No mold cleaning equipment</td>
</tr>
<tr>
<td valign="top" align="left"/><td valign="top" align="left">Plastic scratches</td>
<td valign="top" align="left">Plastic scratches</td>
<td valign="top" align="left">Workers&#x2019; incorrect operation</td>
</tr>
<tr>
<td valign="top" align="left">Wire winding</td>
<td valign="top" align="left">Wire winding failure</td>
<td valign="top" align="left">Improper winding</td>
<td valign="top" align="left">Incorrect tension and number of turns.</td>
</tr>
</tbody>
</table></table-wrap>
</sec>
<sec id="S7">
<title>Improve</title>
<p>After determining the root causes of the problem, solutions to solve the problem were as shown in <xref ref-type="table" rid="T7">Table 7</xref>.</p>
<table-wrap position="float" id="T7">
<label>TABLE 7</label>
<caption><p>The root causes and solutions to solve the problem.</p></caption>
<table cellspacing="5" cellpadding="5" frame="hsides" rules="groups">
<thead>
<tr>
<td valign="top" align="left">Root causes</td>
<td valign="top" align="left">Solutions</td>
</tr>
</thead>
<tbody>
<tr>
<td valign="top" align="left">High mold temperature during production</td>
<td valign="top" align="left">&#x2013; Plan to clean the mold periodically.<break/>&#x2013; Plan to check mold temperature at the beginning and middle of the shift.<break/>&#x2013; Warning when the temperature is outside the allowable limit.</td>
</tr>
<tr>
<td valign="top" align="left">No drying time recorded on the drying drum</td>
<td valign="top" align="left">&#x2013; Determine and display drying time in the drying bin.<break/>&#x2013; Training &#x0026; job guidance.</td>
</tr>
<tr>
<td valign="top" align="left">Inappropriate gloves</td>
<td valign="top" align="left">&#x2013; Use suitable gloves, with the rubber part above the fingertips.<break/>&#x2013; Change gloves periodically.</td>
</tr>
<tr>
<td valign="top" align="left">No mold cleaning equipment</td>
<td valign="top" align="left">Use an air spray gun to clean the mold to blow away any metal particles before inserting the coil and after removing the product.</td>
</tr>
<tr>
<td valign="top" align="left">Workers&#x2019; incorrect operation</td>
<td valign="top" align="left">&#x2013; Worker training.<break/>&#x2013; Regularly check workers&#x2019; operations when taking out products.</td>
</tr>
<tr>
<td valign="top" align="left">Incorrect tension and number of turns</td>
<td valign="top" align="left">DOE</td>
</tr>
</tbody>
</table></table-wrap>
<p>Improvement solutions were specifically described in <xref ref-type="table" rid="T7">Table 7</xref>. The DOE solution at the winding station would be implemented to determine the tension and number of winding turns to minimize the FR at the winding station.</p>
<p>The technical parameters of tension <italic>T</italic> and number of windings <italic>N</italic> of the wire winding process were given in <xref ref-type="table" rid="T8">Table 8</xref>.</p>
<table-wrap position="float" id="T8">
<label>TABLE 8</label>
<caption><p>Technical parameters of the wire winding process.</p></caption>
<table cellspacing="5" cellpadding="5" frame="hsides" rules="groups">
<thead>
<tr>
<td valign="top" align="left">Parameters</td>
<td valign="top" align="center">Specification tolerance</td>
</tr>
</thead>
<tbody>
<tr>
<td valign="top" align="left"><italic>T</italic> (g)</td>
<td valign="top" align="center">550&#x2013;650</td>
</tr>
<tr>
<td valign="top" align="left"><italic>N</italic> (turns)</td>
<td valign="top" align="center">625&#x2013;635</td>
</tr>
</tbody>
</table></table-wrap>
<p>The experiment was performed with two input variables and one output variable. The input variables or factors were tension <italic>T</italic> and number of windings N. The output variable was the station&#x2019;s FR. Tension <italic>T</italic> was tested with seven levels, number of winding <italic>N</italic> was tested with four levels, as shown in <xref ref-type="table" rid="T9">Table 9</xref>.</p>
<table-wrap position="float" id="T9">
<label>TABLE 9</label>
<caption><p>Input factors and their levels.</p></caption>
<table cellspacing="5" cellpadding="5" frame="hsides" rules="groups">
<thead>
<tr>
<td valign="top" align="left">Factors</td>
<td valign="top" align="center">Factor levels</td>
</tr>
</thead>
<tbody>
<tr>
<td valign="top" align="left"><italic>T</italic> (g)</td>
<td valign="top" align="center">570, 580, 590, 600, 610, 620, 630</td>
</tr>
<tr>
<td valign="top" align="left"><italic>N</italic> (turns)</td>
<td valign="top" align="center">626, 628, 630, 632</td>
</tr>
</tbody>
</table></table-wrap>
<p>The experiment was carried out with three repetitions in each factor&#x2019;s combination; the total number of experiments was:</p>
<disp-formula id="S7.Ex1"><mml:math id="M1">
<mml:mrow>
<mml:mrow>
<mml:mi>N</mml:mi>
<mml:mo>=</mml:mo>
<mml:mrow>
<mml:mn>7</mml:mn>
<mml:mo>&#x00D7;</mml:mo>
<mml:mn>4</mml:mn>
<mml:mo>&#x00D7;</mml:mo>
<mml:mn>3</mml:mn>
</mml:mrow>
<mml:mo>=</mml:mo>
<mml:mn>84</mml:mn>
</mml:mrow>
<mml:mo>.</mml:mo>
</mml:mrow>
</mml:math>
</disp-formula>
<p>The experimental sequence was conducted randomly. Experimental results were analyzed with the support of Minitab software. The analysis of variance (ANOVA) table was as shown in <xref ref-type="fig" rid="F7">Figure 7</xref>.</p>
<fig id="F7" position="float">
<label>FIGURE 7</label>
<caption><p>The ANOVA table of the experiment.</p></caption>
<graphic mimetype="image" mime-subtype="tiff" xlink:href="bijamr-2025-40-g007.tif"/>
</fig>
<p>From the ANOVA table above, with a significance level &#x03B1; of 0.05, we see that the input factors, as well as the interactions between factors, all affected the FR. The number of turns <italic>N</italic> has the strongest influence, followed by tension <italic>T</italic> and finally the interaction <italic>N</italic>&#x002A;<italic>T</italic> between the number of turns and tension.</p>
<p>The experimental model was validated with the residual run chart in <xref ref-type="fig" rid="F8">Figure 8</xref> and the normal probability pin <xref ref-type="fig" rid="F9">Figure 9</xref>.</p>
<fig id="F8" position="float">
<label>FIGURE 8</label>
<caption><p>Residual run chart.</p></caption>
<graphic mimetype="image" mime-subtype="tiff" xlink:href="bijamr-2025-40-g008.tif"/>
</fig>
<fig id="F9" position="float">
<label>FIGURE 9</label>
<caption><p>Normal probability plot.</p></caption>
<graphic mimetype="image" mime-subtype="tiff" xlink:href="bijamr-2025-40-g009.tif"/>
</fig>
<p>From the graphs, it could be seen that experimental errors varied randomly and followed a normal distribution. Experimental results could be used to determine input variables to optimize output variables.</p>
<p>The contour plot of FR according to tension <italic>T</italic> and number of windings <italic>N</italic> was shown in <xref ref-type="fig" rid="F10">Figure 10</xref>.</p>
<fig id="F10" position="float">
<label>FIGURE 10</label>
<caption><p>The contour plot of FR according to <italic>T</italic> and <italic>N</italic>.</p></caption>
<graphic mimetype="image" mime-subtype="tiff" xlink:href="bijamr-2025-40-g010.tif"/>
</fig>
<p>With the goal of minimizing the FR, the optimal value of the input variables corresponded to the dark blue area in the middle of the chart. This area had the lowest FR (FR &#x003C; 0.01). This optimal region corresponded to a tension that fluctuated slightly around the value 600, and the number of turns was between the values 628 and 629. The selected values were as follows:</p>
<disp-formula id="S7.Ex2"><mml:math id="M2">
<mml:mtable displaystyle="true" rowspacing="0pt">
<mml:mtr>
<mml:mtd columnalign="left">
<mml:mrow>
<mml:mi>T</mml:mi>
<mml:mo>=</mml:mo>
<mml:mn>600</mml:mn>
</mml:mrow>
</mml:mtd>
</mml:mtr>
<mml:mtr>
<mml:mtd columnalign="left">
<mml:mrow>
<mml:mi>N</mml:mi>
<mml:mo>=</mml:mo>
<mml:mn>628</mml:mn>
</mml:mrow>
</mml:mtd>
</mml:mtr>
</mml:mtable>
</mml:math>
</disp-formula>
<p>After applying improvement solutions, the FRs before and after improvements at the two critical stations, external plastic injection and wire winding, were estimated as shown in <xref ref-type="table" rid="T10">Table 10</xref>. The remaining stations had unchanged FRs.</p>
<table-wrap position="float" id="T10">
<label>TABLE 10</label>
<caption><p>The FRs before and after improvements.</p></caption>
<table cellspacing="5" cellpadding="5" frame="hsides" rules="groups">
<thead>
<tr>
<td valign="top" align="left">i</td>
<td valign="top" align="left">Work stations</td>
<td valign="top" align="center" colspan="2">FR (%)<hr/></td>
</tr>
<tr>
<td/>
<td/>
<td valign="top" align="center">Before</td>
<td valign="top" align="center">After</td>
</tr>
</thead>
<tbody>
<tr>
<td valign="top" align="left">1</td>
<td valign="top" align="left">External plastic injection</td>
<td valign="top" align="center">5.21</td>
<td valign="top" align="center">2.71</td>
</tr>
<tr>
<td valign="top" align="left">2</td>
<td valign="top" align="left">Wire winding</td>
<td valign="top" align="center">3.86</td>
<td valign="top" align="center">1.42</td>
</tr>
<tr>
<td valign="top" align="left">3</td>
<td valign="top" align="left">Soldering</td>
<td valign="top" align="center">0.64</td>
<td valign="top" align="center">0.64</td>
</tr>
<tr>
<td valign="top" align="left">4</td>
<td valign="top" align="left">Inspection of internal diameter &#x0026; appearance</td>
<td valign="top" align="center">0.15</td>
<td valign="top" align="center">0.15</td>
</tr>
<tr>
<td valign="top" align="left">5</td>
<td valign="top" align="left">Excess copper wire processing</td>
<td valign="top" align="center">0.10</td>
<td valign="top" align="center">0.10</td>
</tr>
<tr>
<td valign="top" align="left">6</td>
<td valign="top" align="left">Terminal stamping</td>
<td valign="top" align="center">0.04</td>
<td valign="top" align="center">0.04</td>
</tr>
<tr>
<td valign="top" align="left">7</td>
<td valign="top" align="left">Inspection &#x0026; packaging</td>
<td valign="top" align="center">0.08</td>
<td valign="top" align="center">0.08</td>
</tr>
<tr>
<td valign="top" align="left">8</td>
<td valign="top" align="left">Core stamping</td>
<td valign="top" align="center">0.06</td>
<td valign="top" align="center">0.06</td>
</tr>
<tr>
<td valign="top" align="left">9</td>
<td valign="top" align="left">Terminal assembly</td>
<td valign="top" align="center">0.06</td>
<td valign="top" align="center">0.06</td>
</tr>
<tr>
<td valign="top" align="left">10</td>
<td valign="top" align="left">Core stamping</td>
<td valign="top" align="center">0.06</td>
<td valign="top" align="center">0.06</td>
</tr>
<tr>
<td valign="top" align="left">11</td>
<td valign="top" align="left">Bobin plastic injection</td>
<td valign="top" align="center">0.03</td>
<td valign="top" align="center">0.03</td>
</tr>
<tr>
<td/>
<td valign="top" align="left"><bold>Total</bold></td>
<td valign="top" align="center"><bold>10.27</bold></td>
<td valign="top" align="center"><bold>5.33</bold></td>
</tr>
</tbody>
</table></table-wrap>
<p>It is seen that after improvement, FR decreased from 10.27 to 5.33%, achieving the set goal of reducing FR to less than 6%.</p>
</sec>
<sec id="S8">
<title>Control</title>
<p>Process control was carried out at the injection and winding stations to maintain improved results.</p>
<sec id="S8.SS1">
<title>Control in plastic injection station</title>
<p>At the plastic injection station, the controlled quantities included the plastic injection FR and the plastic layer thickness. The plastic injection FR was controlled by the proportional chart proportional control chart (PCC) 01 with variable control limits. Data were collected, control limits were established, and the PCC 01 chart for controlling the injection FR was shown in <xref ref-type="fig" rid="F11">Figure 11</xref>.</p>
<fig id="F11" position="float">
<label>FIGURE 11</label>
<caption><p>PCC 01 chart for controlling the injection FR.</p></caption>
<graphic mimetype="image" mime-subtype="tiff" xlink:href="bijamr-2025-40-g011.tif"/>
</fig>
<p>The plastic layer thickness was controlled by a pair of variable control charts, including sample mean chart mean control chart (XCC) and sample standard deviation chart standard deviation control chart (SCC). XCC was used to control the layer thickness expectation; SCC was used to control the layer thickness variability. Data were collected, control limits were established, and the control charts were as shown in <xref ref-type="fig" rid="F12">Figure 12</xref>.</p>
<fig id="F12" position="float">
<label>FIGURE 12</label>
<caption><p>Control charts for controlling the layer thickness.</p></caption>
<graphic mimetype="image" mime-subtype="tiff" xlink:href="bijamr-2025-40-g012.tif"/>
</fig>
</sec>
<sec id="S8.SS2">
<title>Control in winding station</title>
<p>At the winding station, the controlled characteristic was the winding FR. The winding FR was controlled by the proportional chart PCC 02 with variable control limits. Data were collected, control limits were established, and the PCC 02 chart for controlling the winding FR was shown in <xref ref-type="fig" rid="F13">Figure 13</xref>.</p>
<fig id="F13" position="float">
<label>FIGURE 13</label>
<caption><p>PCC 02 chart for controlling the winding FR.</p></caption>
<graphic mimetype="image" mime-subtype="tiff" xlink:href="bijamr-2025-40-g013.tif"/>
</fig>
</sec>
</sec>
<sec id="S9" sec-type="conclusion">
<title>Conclusion</title>
<p>The article discusses the application of DOE to improve the coil manufacturing process of the C23 H5 product in the KSVN company. The research methodology was based on Six Sigma thinking, with the platform of the DMAIC procedure. The tools used in the steps of the DMAIC procedure include SIPOC, project charter, cause and effect diagram, Pareto diagram, DOEs, and control charts. After applying Six Sigma tools, the FR of the process reduced from 10.27 to 5.33%, achieving the initially set goal.</p>
<p>DOE had been applied to determine parameters at the winding station to minimize the FR at this station. Control charts had been used in the control phase to maintain improved results by controlling important process characteristics.</p>
<p>Methods discussed in the article still had many limitations. Improvements were only made at plastic injection and wire winding stations. In addition, the control step used only control charts to control important process variables. Further development includes implementing improvements at the remaining stations to further improve the sigma level of the production process and using statistical tools to control the entire process.</p>
</sec>
</body>
<back>
<sec id="S10" sec-type="funding-information">
<title>Funding</title>
<p>The research was not funded from any source.</p>
</sec>
<sec id="S11">
<title>Conflict of interest</title>
<p>The authors report no conflict of interest concerning the materials or methods used in this study or the findings specified in this paper.</p>
</sec>
<ref-list>
<title>References</title>
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