1. Introduction
The company under study specializes in producing garment products. The main products of the company include men vestons, jackets, shirts, and trousers. According to statistics, the average on-time delivery percentage of the company in the past is 85%. It is low and does not meet the expectation of the company leaders. Through analysis, the cause of the problem is due to a long production time, low productivity, and a high defect rate.
This paper uses Lean Six Sigma tools to solve the problem of low on-time delivery through reducing the production time, increasing productivity, and improving the defect rate. The research is carried out on a product with the highest demand on a line of the shirt garment production area.
2. Literature review and research methodology
Lean Six Sigma is the fastest way to improve time and quality; therefore, we can minimize operation costs, minimize capital investment, increase value, and increase customer satisfaction. Lean Six Sigma is an integrated approach of Lean Manufacturing and Six Sigma. If we use Lean Manufacturing alone, we cannot control the process and solve quality problems in the best way. If we use only Six Sigma, we cannot minimize the time, cost, and capital investment. Simultaneous use of Lean and Six Sigma tools helps us achieve high quality, high-speed production, and low cost with breakthrough improvements in a short time. Lean Six Sigma gives faster results than either Six Sigma or Lean Manufacturing.
The research methodology is based on Lean Six Sigma theory, with the platform of DMAIC procedure (1), including five steps:
(1). Define
(2). Measure
(3). Analyze
(4). Improve
(5). Control.
The define step defines the problem, objective, and scope of the study. In this step, the objective is defined qualitatively. The measurement step collects data, maps the current state value stream, identifies current performance indexes, and sets objectives quantitatively. The analysis step finds out the root causes of the problem and then identifies solutions and tools to solve the problems. The improvement step implements solutions to improve the process in order to achieve the objectives. The control step controls the improved process to maintain improved results.
The tools used in the steps of DMAIC procedure include value stream management, work design, SMED, line balancing, Kanban, FIFO, autonomous maintenance, visual management, design of experiments (DOE), and control charts. All tools used can be found in references (1) and (2), along with articles (3) and (4).
3. Define
The problem that the company encounters is a low percentage of on-time delivery. The average on-time delivery percentage of the company is 85% and needs to be improved. Through analysis, the cause of the problem is due to a long production lead time, low productivity, a high cycle time, or a high defect per unit rate. The research is carried out on a product family with the highest demand (5, 6). The SIPOC diagram of the product family is as in Figure 1.
This paper focuses on the process of back finish with six stations as in Table 1.
The defined stage is summarized in the project charter as in Table 2.
4. Measure
The collected data in the back finish process, including number of workers n, change over time (COT), cycle time (CT), lead time (LT), and defect per unit (DPU), are shown in Table 3.
Currently, the company works 6 days/week, 1 shift/day, 8 h/shift. The average break time is 40 min/day. The average COT is 65 min/day. The available producing time is as follows:
with the demand of 1500 pcs/day. The talk time TT is calculated as follows:
Work in process inventory WIP and time in process TIP are calculated and shown in Table 4.
With the data above, the current state map of the process is as in Figure 2.
From the map, the current indexes, their values, and performance assessment are as in Table 5.
The objectives of the research are set as in Table 6.
5. Analyze
5.1. Analyze the long-time problem
The long-time problems are demonstrated by long LT and long CT, exceeding the TT. The balance chart is as in Figure 3.
The process is unbalanced, leading to the increase of WIP inventory, causing long LT. Besides, CT of the process is 25 s, higher than TT, which is 15 s; the current production rate does not meet the demand rate. The causes of the problem are analyzed through the fish bone diagram as in Figure 4.
From the diagram, the causes, solutions, and solving tools are demonstrated in Table 7.
5.2. Analyze the high-defect problem
The causes of high-DPU problems are analyzed through the fish bone diagram as in Figure 5.
The Pareto charts for the causes are as in Figure 6.
The fish bone diagram for the skip stitch shoulder effect is as in Figure 7.
The fish bone diagram for the skip stitch yoke effect is as in Figure 8.
From the fish bone diagrams, the causes, solutions, and solving tools for skip stitch shoulder and yoke defects are presented in Table 8.
The fish bone diagram for the broken stitch shoulder defects is as in Figure 9.
From the fish bone diagrams, the causes, solutions, and solving tools for broken stitch shoulder defects are presented in Table 9.
6. Improve
6.1. Quick change over SMED
Change over time needs to be reduced to lift up TT. Based on (2), SMED is used by the following steps.
Step 1: Identify time elements.
Elements and their time are collected, as in Table 10.
Step 2: Separate external elements
The internal and external elements are separated as in Table 11.
Step 3: Convert internal elements to external elements.
The internal elements are converted to external elements as in Table 12.
Step 4: Streamline remaining elements
The remaining elements are streamlined as in Table 13.
After using SMED, COT, APT, and TT change as in Table 14.
The balance chart of the process after using SMED is as in Figure 10.
The process CT is 25 s, still higher than TT. Work design needs to be used to reduce the CT of each station to meet the TT.
6.2. Work design
Collecting the working elements of each station and their processing time is as in Table 15.
By analyzing and removing wasted motion, reallocating the work load of the right and left hands, designing support tools, and rearranging station layout, the results are that the CT reduced while the number of workers remained unchanged, as shown in Table 16.
The balance chart after using work design is as in Figure 11.
The process CT is now 19 s, which still exceeds the TT, 16.8 s. Line balancing is used to reallocate work load of each station to meet demand.
6.3. Line balancing
Applying the line balancing model in (3), we reallocate the work load and worker for the stations with constraints of the element order and the goal of meeting TT. The results are as in Table 17.
The balance chart after using line balancing is as in Figure 12.
The process CT now is 16.5 s, which meets the TT, 16.77 s. On the other hand, the number of workers has reduced to 8, the number of stations has reduced to 5, and the line balancing efficiency has increased to 92.12%. The process is more balanced, but we still have to control WIP inventory.
6.4. WIP inventory control
With reference to (1), in order to control WIP, Kanban systems would be placed between stations 2 and 3 and between stations 4 and 5. FIFO lanes would be placed between stations 1 and 2 and between stations 3 and 4.
Applying Kanban models in (1), the numbers of Kanban cards, N, are calculated, as in Table 18, with the demand D of 1500 products, a lot size Q of 5, and α = 0.1. The formula of N is as below:
According to models in (4), the FIFO lane sizes, S, are calculated as in Table 19.
6.5. Autonomous maintenance
In order to solve the causes of machine failures, machines have been restored to their basic conditions. AM activities are then established by the following steps.
Step 1: A standard checklist for routine cleaning, inspection, and lubrication activities is established as in Table 20.
Step 2: Establish needle and thread inspection standards as in Table 21.
Step 3: Design checking notes for cleaning, inspection, and lubrication as in Table 22.
6.6. Visual control
In order to solve needle-size-not-appropriate problems, a visual tool has been used by matching size needles with colors. Also, we put them in the same color boxes. Depending on needle sizes, the storage capacity of each box is determined as in Table 23.
6.7. Thread storage system design
A low-quality thread is one of the most important causes which lead to broken stitch problems. By using 5-Why analysis, the root cause is identified, that is, the storage time of the thread. The quality of long-time-storage threads has been reduced. To solve the problem, a thread storage system has been designed to determine the storage time as in Figure 13. This system contains three types of cards:
– Time card: Cards indicate the storage date of the material.
– Empty card: Cards attached on empty batches.
– Emergency red card: This is the only card that is attached on the longest storage time batch, which is priority for using.
The operational process is as follows:
– Import materials are stored in the empty batch (with empty cards).
– Then, empty cards are replaced with time cards with storage dates of the batch.
– Emergency cards with the longest storage time batch.
– In case of stocking out batches (with emergency cards), they are replaced with empty cards.
6.8. Design of experiments
With reference to (1), DOE is implemented in the Yoke Station to minimize skip stitch errors and in the Shoulder Station to minimize skip stitch and broken stitch errors.
6.8.1. Yoke station
The input variables are needle eye stock, rotary hook distance D, and amount of taken thread A. The output variable is the skip defect rate DR. The variables are shown in Figure 14.
The levels of factors are defined as in Table 24.
With the number of repetitions of 3, the number of experiments is 36. The data are collected. From the collected data, the ANOVA is shown as in Table 25.
Through ANOVA analysis, both factors and their interaction have affected defect rate. The contour plot of defect rate DR according to the amount of taken thread A and the distance of needle eye stock and rotary hook D is shown in Figure 15.
From the plot, the distance of needle eye stock and rotary hook D should be between 1.6 mm and 2.1 mm, and the amount of thread taken A should be set up from the level of 3.5 to 4.5. The value of the distance of 2 mm and the amount of thread taken of level are chosen.
6.8.2. Shoulder station
The input variables are needle eye stock, rotary hook distance D, amount of taken thread A, and thread tension T. The output variable is the skip defect rate DR. The variables are shown in Figure 16.
The levels of input factors are defined as in Table 26.
With the number of repetitions of 2, the number of replicas is 36. The data are collected. From the collected data, the ANOVA is shown as in Table 27.
Through ANOVA analysis, both factors and their 2-factor interaction have affected the defect rate. The interaction plot is shown in Figure 17.
From the plot, the lowest defect rate would be attained with a distance of 2 mm, a tension level of 3, and a thread taken level of 3.
The results of applying DOE are shown in Table 28.
6.9. Future state map
After applying Lean Six Sigma tools, the future state map is as in Figure 18.
From the map, the system indexes are presented as in Table 29.
A comparison of the performance indexes of the current state map CSM and the future state map FSM is shown in Table 30.
The result shows that all the performance indexes have been improved.
7. Control
In order to maintain improved results, the control charts of important system parameters, LT, CT, and DPU, would be developed. With the current data, the control charts are constructed and operated. The LT control chart is as in Figure 19.
The CT control chart is as in Figure 20.
The DPU control chart is as in Figure 21.
8. Conclusion
The research has implemented Lean Six Sigma to improve a garment production process. The research methodology is based on the platform of DMAIC procedure, including five steps: define, measure, analyze, improve, and control. The tools used in the steps of DMAIC procedure include CED, Pareto diagram, value stream management, work design, SMED, line balancing, Kanban, FIFO, autonomous maintenance, visual management, DOE, and control charts.
After applying Lean Six Sigma tools, the company has reduced the production lead time by 89.21% from 279 to 30.1 min, reduced the production cycle time by 36% from 25 to 16 s, reduced the process defect rate by 37.45% from 14.9 to 9.32%, and then improved the on-time delivery rate. The results show that the research has met the objectives with the advantages of following strict and scientific methodology and using many tools; among them are strong tools like DOE.
The research still had some disadvantages. The number of collected samples used in DOE is small. The control phase has not built up standard operating processes for controlling the whole process. The improvements have not been implemented to verify the effectiveness of research. These restrictions would guide the way for future research.
Author contributions
PNN is the thesis advisor of PH, PTN, and QD. PN has developed the models for the thesis. PH, PTN, and QD have collected and analyzed the data and run the models. PNN has composed the article based on the thesis. All authors contributed to the article and approved the submitted version.
Acknowledgments
We extend our heartfelt appreciation to everyone who has contributed to the completion of this research article, especially our families, Ho Chi Minh City University of Technology (HCMUT), and the scientific community, for their invaluable support.
Conflict of interest
The research is conducted in the absence of any commercial or financial relationships that could be construed as a potential conflict of interest.
References
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5. Phong NN, Phuc NH, Thanh VV, Sang NV, Hai NV, Hoa NV. Applying lean six sigma to improve productivity and quality of production systems – A case study in the Kia Cabin Welding Line, Model K2700ii & K3000s. J Sci Technol Dev. (2015) 18.